Ian
Notorious member
Not to worry, it was a $2 Chinese brazed carbide jobbie that I had to re-profile to make work anyway.
The point is really about barrel quality. Most shooters probably have no idea how badly the bores of their rifles can be "hooked", or curved, or how much the OD can be non-concentric with the bore centerline. So I have this Savage .308 sporter barrel that was given to me, an un-fired take off barrel which clearly had a hook in the bore about 4-5" back from the muzzle and was destined to become a jack handle pending me getting a lathe to turn the end to the correct diameter. I decided to cut it down to 16.5" and thread it for practice instead. After indicating the inside of the chamber to zero in my outboard spider and a pin I turned to fit the bore indicated true in the muzzle, I checked the OD of the barrel (which looked pretty loopy from what little I could see sticking out of the chuck) at both ends. .007" TIR in front of the nut and .006" at the muzzle, not great but not terrible.
So I got my parting tool set up to lop it off at 16.6" and had a go. Interrupted cut deluxe. Anyway, it seemed prudent to stop just short of the groove diameter minus a fudge factor approximating the eccentricity of the OD and finish with a hack saw since I'd never done this before, but I underestimated the amount of hook the bore made inside the already wongo outside (the barrel OD was actually pretty straight when rolled on a sheet of glass), so my fudge factor was insufficient to keep the tool from breaking through suddenly on a groove before I reached my pre-determined whoa-up and grab the hacksaw point. Of course with the wongomatic bore the heavily-loaded tool dug in and snapped off.
Lesson well learned.
Turns out the bore at that particular spot in the barrel was .042" off center with the OD. Remember that before parting it off I had zeroed the bore at the muzzle, just 5.4" ahead of this point, but at the cut it was running about .035" off center. See why this brand-spanking new barrel was supposed to be a jack handle? Actually it might be OK now that I cut the worst part off, crowned it, and threaded it, but with the barrel being .654" there's almost no shoulder on one side of it so putting a suppressor on it would be an iffy proposition and only really possible if one put a thick washer against the shoulder and slid it over to center on the OD instead of the threads.
Before anyone busts my butt, I repeat this was a known JUNK barrel to begin with, so no I didn't put any brass pads or copper wire between the chuck jaws and barrel as I would when turning a good one.
The good news is I learned something, didn't hurt anything important, and got to trial run my outboard spider and new 4-jaw chuck which both worked like a dream. As a bonus maybe some of you will find the photo interesting.
The point is really about barrel quality. Most shooters probably have no idea how badly the bores of their rifles can be "hooked", or curved, or how much the OD can be non-concentric with the bore centerline. So I have this Savage .308 sporter barrel that was given to me, an un-fired take off barrel which clearly had a hook in the bore about 4-5" back from the muzzle and was destined to become a jack handle pending me getting a lathe to turn the end to the correct diameter. I decided to cut it down to 16.5" and thread it for practice instead. After indicating the inside of the chamber to zero in my outboard spider and a pin I turned to fit the bore indicated true in the muzzle, I checked the OD of the barrel (which looked pretty loopy from what little I could see sticking out of the chuck) at both ends. .007" TIR in front of the nut and .006" at the muzzle, not great but not terrible.
So I got my parting tool set up to lop it off at 16.6" and had a go. Interrupted cut deluxe. Anyway, it seemed prudent to stop just short of the groove diameter minus a fudge factor approximating the eccentricity of the OD and finish with a hack saw since I'd never done this before, but I underestimated the amount of hook the bore made inside the already wongo outside (the barrel OD was actually pretty straight when rolled on a sheet of glass), so my fudge factor was insufficient to keep the tool from breaking through suddenly on a groove before I reached my pre-determined whoa-up and grab the hacksaw point. Of course with the wongomatic bore the heavily-loaded tool dug in and snapped off.
Lesson well learned.
Turns out the bore at that particular spot in the barrel was .042" off center with the OD. Remember that before parting it off I had zeroed the bore at the muzzle, just 5.4" ahead of this point, but at the cut it was running about .035" off center. See why this brand-spanking new barrel was supposed to be a jack handle? Actually it might be OK now that I cut the worst part off, crowned it, and threaded it, but with the barrel being .654" there's almost no shoulder on one side of it so putting a suppressor on it would be an iffy proposition and only really possible if one put a thick washer against the shoulder and slid it over to center on the OD instead of the threads.
Before anyone busts my butt, I repeat this was a known JUNK barrel to begin with, so no I didn't put any brass pads or copper wire between the chuck jaws and barrel as I would when turning a good one.
The good news is I learned something, didn't hurt anything important, and got to trial run my outboard spider and new 4-jaw chuck which both worked like a dream. As a bonus maybe some of you will find the photo interesting.
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