L Ross
Well-Known Member
A couple weekends ago my friend Charlie came over and helped me make .357 Herrett brass, then loaded ammo, and finally shot the same. I have an unmarked aluminum two cavity .35 caliber mould that drops a 215 semi pointed bullet at .359 but was lop sided, eccentric, out of round, and was prone to air bubbles exposed in a lube groove.
Today I sat down with my Opti-Visor and a pair of cheaters and really gave it a hard examination. I soaked the back sides of the alignment pins and waited about 15 minutes while I scrounged up a flat tipped punch and a ball pein hammer. As soon as the pins moved the lop sided cavities lined up almost perfectly. I could not see any blocked venting. I hunted around and found a set of stainless handles from Dick Dastardly made to fit Lee six cavity blocks. These handles are very well made. I took the RCBS handles off and put the DD handles on and had noticeably less slop in the system.
Fired up the pot with WW set the same as I left it from casting the 32 lbs. of RCBS 35-200-FN. Pre-heated the mould on a hot plate thenstarted casting as fast as I could. Good bullets started dropping right away, but I still discarded some until the color stabilized, i.e. equally hint of almost frosting. Boy the aluminum mould sheds heat a lot faster than the iron RCBS. No need for the manicurist's fan at all. Now the bullets were round, later proven when I ran them through a sizer and there is equal contact all the way around. And surprise surprise, no more venting issues. Ran off 8 1/2 lbs. waiting for the UPS truck to drop off 10 lbs. of Biloxi Shrimp Co. shrimp.
Today I sat down with my Opti-Visor and a pair of cheaters and really gave it a hard examination. I soaked the back sides of the alignment pins and waited about 15 minutes while I scrounged up a flat tipped punch and a ball pein hammer. As soon as the pins moved the lop sided cavities lined up almost perfectly. I could not see any blocked venting. I hunted around and found a set of stainless handles from Dick Dastardly made to fit Lee six cavity blocks. These handles are very well made. I took the RCBS handles off and put the DD handles on and had noticeably less slop in the system.
Fired up the pot with WW set the same as I left it from casting the 32 lbs. of RCBS 35-200-FN. Pre-heated the mould on a hot plate thenstarted casting as fast as I could. Good bullets started dropping right away, but I still discarded some until the color stabilized, i.e. equally hint of almost frosting. Boy the aluminum mould sheds heat a lot faster than the iron RCBS. No need for the manicurist's fan at all. Now the bullets were round, later proven when I ran them through a sizer and there is equal contact all the way around. And surprise surprise, no more venting issues. Ran off 8 1/2 lbs. waiting for the UPS truck to drop off 10 lbs. of Biloxi Shrimp Co. shrimp.